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KUKA - Simulated movements are different than actual movements

#1
Question
Greetings,

Problem:
The simulated movements work, but after transferring the files to the robot, the movements do not work. The robot moves to the desired start position, then makes a completely incorrect movement, often ending in a physical crash (not damage, going slow and monitoring).

Setup:
A KRC4 controller, a KL 100 linear positioner (E1), a KR 10 R1100 sixx. The ultimate goal is to have it 3d print.

Attachments:
-The RDK station (ignore the floating robot, that is by design; the linear positioner has '0.000' set in the center of the rail.
——生成的3 d打印课题ams (the odd movements also occur with regular movements between targets.


Thank you,
Adam


Attached Files
.src Print3D.src(Size: 140.33 KB / Downloads: 252)
.rdk Baby_Kuka-Linear_Rail.rdk(Size: 10.53 MB / Downloads: 284)


Messages In This Thread
KUKA - Simulated movements are different than actual movements - byadam_frey- 07-23-2021, 09:21 PM



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